A belated log of the SDL's life with us.
...
Friday, October 22, 2004
Last night as my wife drove home from orchestra rehearsal (late), a
deer T-boned her in the SDL. She said she saw horns, so it was
probably one of the larger bucks that are running around. (Scared
too, now that it's deer season.) Took out the driver's side mirror
glass (which scratched the side window as it slammed into it), put a
small crease in the rear door, and wiped out the wraparound part of
the taillight on that side. And put a very deep dent in the metal
just in front of the taillight. Broken paint, etc. Messed up the
hole where the light goes, so it wouldn't be watertight even with a
new light assembly. The mirror housing look OK, at least. The side
crease is probably a paintless dent candidate. But that bowling-ball
sized dent in the back is trouble.
That car's a magnet for trouble it seems. We don't run comprehensive
insurance on it, so this one will be on us.
Sigh.
Monday, November 1, 2004
Took the car to the paintless dent repair place, which had the best
quote (by far) for repairing the body damage. First looks had missed
the fact that the deer nailed the front fender, both doors, and the
rear fender. And the mirror and tail light.
Tuesday, November 2, 2004
The vacuum pump on the SDL is now making noises worse than the
original (?) one I replaced 27 kmi ago that went 228 kmi.
I did not remove the assembly basket, and I used the non-dam
gasket. Same situation as that which had gone so many miles, in other
words. It worked well and sounded good, but now it's making a bad
clattery sucky noise, much like the original one did as it went bad.
No sign of malfunction yet, other than the noise. But if it's bad
enough that it alarms my wife, it's bad!
The car's in the body shop right now, but when it comes back I may
keep the wife in the Chicken Wagon while I investigate the issue. I
still have the original pump, whose only problem was a loose cover
that perhaps I could secure. I also have a used pump that I could
try, because I'm sure not interested in dropping $200 a year on vacuum
pumps!
It seems odd to me that a failure could have been caused by the
presence of the basket, since they didn't fail like this
originally. The pump looks the same, except for the extra screws in
the cover and the shrouded bearing. I left the basket in because I
knew it'd get misplaced if it wasn't.
Thursday, November 4, 2004
Got the car back from the paintless dent repair place, which also will
do more traditional bodywork. They fixed all four dented panels:
three paintless, and one requiring paint etc. Looks pretty good,
probably about as good as the car did before. Total bill: $500. I
still have to replace the broken mirror glass, the tail light lens,
and the pinstriping on the rear quarter. 'Good enough' for 1/3 the
price, sounds OK to me.
Also, the horrid vacuum pump noise is getting worse, so the car will
be benched until I can address it.
Thursday, November 18, 2004
I finally had a chance to look at the noisy SDL, if only for a few
minutes. I put it in the garage and popped the hood while it was
running. It wasn't being too noisy at the time, but it wasn't
sounding perfectly happy either. I can tell you it's not the cover on
the (new) vacuum pump, but I'm not sure what it is. It's not the fan
shroud rubbing the fan either. But what noise there was seemed to be
more from the fan and/or clutch area, but that's really hard to be
sure of. And there may or may not be more play in the fan clutch than
there ought to be. I'll really have to dig into this some more. But,
it's at the top of the list right now, so it should get dealt with
fairly quickly.
The replaced-with-new parts list is: tensioner, fan, clutch,
water pump, vacuum pump, belt. Not much left in that area.
Saturday, November 27, 2004
I got a chance to dig into the SDL this (long) holiday weekend. It is
not the tensioner shock or its spring. Nor did it appear to be the
vacuum pump, once I got the car warmed up so that it was good and
noisy and had a little snoopy listen. Nothing was immediately
obvious, so I removed the fan, clutch, shroud, and belt. Then I
notice the smoking gun: the (new) tensioner was loose. The big bolt,
in spite of being lock-tited, had worked halfway loose. I don't think
that it had seriously chewed up the timing cover yet, I'm sure hoping
that this is so anyway. At least, in the worst case I should have a
spare timing cover from the wagon. That'd probably nearly pay for its
procurement right there.
What disturbs me is that the 'new' tensioner now has a lot of slop in
the bearing. As much as the old one that I replaced. (Though the old
one's bearing is also gritty and crunchy.) The bearing is still
smooth, but it's all greasy like the seal has failed too. I'm not
sure what to do there, whether it's OK or whether I need to procure
another one. (If I do, I might pursue just replacing the
bearing in it.) Anybody got an opinion on that? How could its bolt
working loose have caused bearing failure so soon?
What's this? More 'smoke'? Hey, another smoking gun! It seems to me
that you shouldn't be able to grab onto the crank pulley and rattle it
back and forth by hand. No, that's just wrong. The bolts holding the
pulley and balancer to the big flange were loose, so I removed them.
Many bolts were chewed through the threads by the rattling loose
pulley. Now, that will make a bit of noise! The phasing pin
is a little chewed too, but I think we'll just ignore that. I need to
get some more bolts to replace the chewed ones, I might even have some
in the parts car.
But wait, there's more. One of the bolts had lost its head, and was
sinking into the flange under vibration. And had made it far
enough out the other side to start milling a groove into the face of
the timing cover! Aluminum flakes everywhere. Now that will
really make a bit of noise! It hadn't gotten far enough to
cause any lasting trouble, though. Good thing I took it away from my
wife when I did! Completely explains the occasional nasty squeaking
noise that would happen.
This poor car. Got a death wish, it does. I don't know if we'll be
able to mount a successful suicide watch on it or not. But at least
we'll be able to put it back together again with no lasting harm from
this attempt. (As soon as I decide what to do about the tensioner.)
Saturday, December 11, 2005
I put the SDL back together. The (2) new belt tensioner bearings I
bought were 12mm thick, to replace the (1) 30mm original bearing.
That meant I had to come up with 6mm of spacer, which I made out of
two 3mm thick fender washers in which I burned a bigger center hole
with the torch. Messy job, and I probably need to re-do it at some
time, since it turned out a little too thick and the circlip wouldn't
go in. But I need a new belt anyway, and I'll tackle it again when it
comes in.
The car runs fine. I stole 'new' bolts for the crank pulley from the
87 TD parts car. Also a plastic dust cap for the idler wheel.
(The tensioner cap was gone.) I never knew I was supposed to have
them!
Monday, January 17, 2005
Today the thaw hit, and the hill up to our house became a skating
rink. I couldn't make it up in the Frankenheap (no real surprise there), and
lost one of my new POS fog lights trying. (I recovered it, a bit of
Shoe Goo ought to put it right.)
My wife couldn't make it up in the SDL either, and it has studded
Hakkapeliitta 1's on it. That was more of a surprise. I managed to
drive her up to the top in the 4wd pickup truck, but it was dicey. I
walked back down the hill to take a stab at driving the SDL up, at
least to the neighbor's driveway, rather than leave it on the main
road all night. I take the hills a bit more aggressively than she
does.
Anyway, a dog picked the worst possible moment to dart onto the road,
no possible way to avoid it, and I hit it very hard. Lost the grille
and the aux fan, or at least its shield, and may or may not have lost
the AC condenser. Everything else looks OK. And yes, the dog is now
an ex-dog. Very unenjoyable situation, especially as I think this is
the second dog of these particular neighbors that I've run over there.
[It's not their dog, it turns out.]
What luck we've had with that car. I think it's drivable though, and
I plan to Shoe-Goo the plastic pieces together until they can be
properly replaced.
Tuesday, January 18, 2005
This morning I walked the road where I hit the dog, and found some
more small pieces of the grille. Looks like I now have most of it.
Can't work on either damaged car, because they're both at the
neighbors' and not in our garage! It's still thawing, it's pointless
to try to bring either car home in the morning. We'll just walk down
to get the cars when we leave, go about our business, and by the time
we come home the road should have thawed to usability.
Wednesday, January 19, 2005
I removed the grille from the car and took it inside to glue together.
Using Shoe Goo, I tacked all the pieces together and set it in a vise
to hold it in shape while it dried. It's going to be a very ratty
repair job, but it's only going to be for a few days. I told Jill to
drive the truck instead today.
This evening, I straightened out the bent aluminum trim pieces, laid
the grill down flat, and glued the trim to it more or less in place.
Thursday, January 20, 2005
Installed the grille. It doesn't grab the eye anymore, though it's
obviously messed up if you actually look at it. There are still
several missing pieces, though they're small. New parts are on order,
this gluing is just temporary to keep rocks out of the more delicate
parts of the car, and to make it marginally more presentable.
Friday, January 21, 2005
Jill was complaining that the car unlocked slowly, and that she could
hear a noise afterwards. I checked, and the pump was running for a
long time after unlocking the car. Locking, it behaved as expected.
Signs of a leaking actuator!
So I got out the MityVac, and more useful, an engine vacuum test
gauge. (This measures both vacuum and pressure, unlike my [older]
MityVac. The MityVac kit's fittings were useful, though. Newer
MityVacs can measure and produce both vacuum and pressure. I'm
thinking I should get one sometime.) I dug into the spare tire well
of the car and liberated the pump from its nest, and teed the gauge
into it. Then, I cycled the locks via the driver's door switch, while
watching the gauge. Yes, it ran 'forever' on the pressure cycle.
(Until timeout.) I corked off the pump itself and cycled it, and it
built pressure/vacuum and stopped immediately. So, the problem was in
the car somewhere, not the pump. (As expected, but it's good to test
your assumptions first before going nuts tearing into the car.)
The next step was to go up to the 4-way splitter at the fuel door
lock. I pulled off the fuel door lock connection and used a golf tee
to plug it. No change. Next, I removed and plugged the connection to
the trunk. Change! The locks behaved properly. Hey, if there has to
be a leak, the trunk actuator is the best one to have. Also, it had
been troublesome before, and I'd in fact sealed its body with RTV
because of leaking. I think its time was up!
More digging liberated this actuator. I restored the other plumbing
to its normal state, and plugged the line at the actuator. The locks
still behaved normally, pinpointing the actuator itself as the
problem.
Last year (?) sometime I'd found a 190E at the U-Pull, and had
extracted from it all the parts of its central locking system (minus
most hoses and wires, of course) to use as spares. I dug this out of
the pile, and it appeared that its trunk actuator, though slightly
different in appearance, would substitute for the SDL's. So, I tied
it into the system, and it worked properly. It was fairly
straightforward to install it, and after I had done so everything
worked properly.
I buttoned up the car and told her it was fixed: for $2! (What I'd
paid for each actuator at the yard.)
Thursday, February 10, 2005
Last week my wife noticed (bless her for watching closely!) the
alternator light flickering on and off, so I told her to quit driving
it and use something else until I could address the issue. (Chicken Wagon to the rescue again!) I figured it
was the brushes going out, and that I'd need to change them. After
all, that's extremely common.
So today I got time to look into it. Examining the situation, it
appears that you need to get at the brush pack from the bottom of the
car, so I jacked it up in preparation for removing the belly pan and
taking out the brush pack for a look-see. While standing around at
the front of the car woolgathering, and looking over the dog damage, I
happened to notice that the belt tensioner spring looked funny. As
in: half there. What an odd optical illusion, I thought. So I looked
closer. Not an odd optical illusion at all, it had broken in half,
and the bottom part was gone! The odd part is that the belt hadn't
derailed. Not yet, anyway. So she hadn't lost engine cooling, nor
did she notice a lack of power steering.
I'm thinking the earlier loose-crank-pulley situation had severely
stressed this spring, which in conjunction with its age (250 kmi)
caused its demise.
Now what's the point of having a parts car for your SDL motor in the
woods, if you don't harvest parts off of it? So I again went to the
300TD, and snagged the tensioner spring off of it and put it on the
car. There, done. I also fished the bottom half of the original
spring off of the belly pan where it had been lying there quietly,
then I let the car down and told my wife that she could drive it again
if she wanted to. I didn't even lose too much time as a result of not
going through a proper diagnosis procedure, just the time I wasted
jacking up the car.
Friday, February 11, 2005
Yesterday the used eBay tail light was delivered, so I installed it
this morning. Easy-squeezy, and no problems with the fit, etc. It
looks good, and fits well, though in the bright sunlight the reverse
lamp is obviously more yellowed than the other (new-ish) one. Thus
ends the suicidal deer episode. Final tally: about $675. Stupid
deer.
Saturday, February 19, 2005
Before leaving for home from my parents house, I washed the car since
it was so filthy. (My wife had been complaining for some time.) We
were going to be taking off immediately so I left the keys in it.
Mistake! My wife went to open the trunk to put in some stuff, and
when she poked the button she heard the car lock itself. WTF? Ain't
supposed to do that. No problem, except that the only set of keys we
had with us, my wife's with the keyless remote, was now locked inside!
(That'll teach me to leave my keys home when I fly.)
OK, that's a big PITA. With the help of my brother (the mechanic) we
were able to pry the door frame open enough using a plastic wedge so
that a piece of bent welding wire could be used to hook the knob,
unlocking the door. Opening the door set off the alarm, but it was an
easy matter to grab the keys and disarm it. This little side-event
only cost us an hour!
One oddity is that the keyless fob no longer seems to work, though it
lights up normally. Perhaps the keyless wart, which lives in the
(leaking) trunk got wet? Will have to investigate when I get more
time, but that's not going to be particularly soon. The car was so
filthy because I told my wife not to wash the car until the
badly-leaking trunk could be dealt with. The deer-broken tail light
was obviously not the only problem. With all the shots to the ass
this car's taken in its life, the trunk lid no longer fits right.
Sunday, February 20, 2005
Yesterday's door-prying sprung the window frame enough that there was
a small wind leak. I he-manned it back into place. Good thing my
wife wasn't watching, it's a brutal procedure!
Monday, March 14, 2005
Having lived with no keyless entry system for about a month, to my
wife's great annoyance, I finally tackled this problem. First I got
out the spare fob, and found that it operated perfectly. Then I
swapped fob batteries, for no apparent change.
Next I retrained the keyless wart with the two fobs' identities.
(It's not entirely obvious when/why to do this from the manual, but I
was able to eventually puzzle it out.) That did the trick. It seems
that the keyless system went insane that morning when it locked us
out, and lost the fob's identity at the same time. No real clue how
this could have happened, it would take a lot of water to drown the
keyless wart where it lives on the side wall of the spare tire well.
Testing after the retraining showed no anomalies.
Since the weather has been so warm lately I think winter is over, so I
swapped back the summer tires. Easier to say than to do! Still takes
less time out of my life to do it myself than to go to the tire shop
and wait for them to do it, even though it's free, and I get exercise
too.
Tuesday, March 15, 2005
Put more PS fluid in. There's definitely a leak, last night it was
groaning again, and this morning the level was down below the filter.
I've been putting off dealing with this, but it's looking like I won't
be able to for much longer.
At least last night at our concert, where I had to get into and out of
the car several times, the keyless entry worked perfectly again.
Saturday, April 2, 2005
While filling up, I had my wife check the mileage since the last oil
change. 5800! (Over my target 5000 mile number. As usual. Man, she
really racks up the miles on this thing.) We were going home, and
then immediately out again to a party. We expected to get back late
enough that I wouldn't be wanting to do this job then, and by morning
(when my wife was going to take a moderate road trip) the oil would be
too cold to suck out easily. So, it was now or never! In a flash I
fired up the topside oil sucker and had it vacuumed out while my wife
was still inside getting ready. I popped the cap off the filter to
let it drain better (I wasn't changing the filter this time, I usually
only do that every other time) and it sucked out pretty quickly since
it was so hot. Not hot enough to collapse the vacuum hose, however,
so it was all OK. While in the area I sucked out the PS reservoir
too, and put in fresh fluid. (With the leak it sometimes runs low and
groans, and the fluid gets pretty mucked up then. It smelled a bit
burnt, so I thought a change was in order.) It didn't take too long
to dump in two gallon jugs of Delo either, and I was just closing the
hood when she came out to the garage to start loading up the car.
She looked surprised, and was impressed at how quickly that job can be
done. Yes, honey, there are a few reasons this car is superior
to your old Escort!
Tuesday, April 5, 2005
Picked up a set of decently-priced used Euro headlights for the car on
eBay, complete with vacuum adjuster stuff. Someday...
Tuesday, April 12, 2005
Today at lunch my wife opened the sunroof at my boy's request, and
when she tried to close it, it jammed! Crap. We were able to fiddle
with it enough to get it closed, but it's definitely broken now. That
won't be any fun to put right.
Sigh. Death-wish SDL indeed.
Wednesday, May 25, 2005
Yesterday and today we went on a 380-mile road trip to Walla Walla,
and I tried for an economy run: I kept it to about 2500 RPM, or a
little less than 60 MPH. The trip down was on slightly slower
secondary roads, while the trip back was on the primary roads but had
the AC on (with minor [but adequate] cooling). The car seemed to like
it, and turned in a respectable 30.2 MPG.
Friday, June 10, 2005
Installed the upgraded keyless entry
system I bought for the car. Easy, and works great. Now both Jill's
SL and this car can be operated from the same fob. The old keyless
unit (still functional) was retired back into its box for later
re-use (maybe). While I was there in the trunk I unplugged the
sunroof motor so we won't accidentally forget that it's broken
and jam it. (And with a three-year-old around, such accidents
are much more likely!)
Also 'tested' the AC system. Again. Seems to be an annual event,
though this year there was still a fair amount of residual pressure.
Enough to cool a little, but not well. Got 45 °F vent
temperatures during the test, although the ambient temperature was
only about 80 °F. Good enough, probably. For whatever
reason (capacity? H-bridge expansion valve?) this car never sees the
low vent temperatures during the test that some of our others do,
though the car is always perfectly comfortable.
Took the car for a shopping trip, and it worked well. It was a
beautiful Friday, and I hit three stores and four garage sales (on the
way back). The AC worked nicely, and the keyless entry system worked
just fine. A success!
Monday, June 13, 2005
While out shopping, we heard a strange scraping noise once when
starting off, it sounded like something to do with the front wheel.
Couldn't find anything wrong, though. Howver, at the very next start
there was an immediate loud scraping noise once the motor was started.
I killed the motor and popped the hood, and found that the fan shroud
had broken (at its thinnest point, of course) and was caught up in the
fan. I was able to bend it out of the way temporarily. It should be
repairable, but WTF!
Tuesday, June 14, 2005
Removed the fan (a real knuckle-buster!) using an allen wrench socket
bit and a box-end wrench over the shaft (no room for the ratchet
wrench), and pulled out the fan shroud. Splinted the break in the
shroud with two pieces of thick sheet metal, and potted the joint with
Shoe Goo.
Wednesday, June 15, 2005
Installed the repaired fan shroud.
Monday, June 20, 2005
Wife picked up a screw in one of the tires somewhere. Took it off and
dropped it off at Les Schwab, and they fixed it gratis. (We bought
the tires there.) Guy said 'tis the season, and they're getting a
lot of screws in tires now due to home improvements.
Thursday, July 28, 2005
This car's not getting driven much in high convertible season, but
today I had it out of the garage so we could do some painting inside,
and I washed the car. As the recycling was building up, the car was
out, and it has a big trunk, I took it to town today to drop off the
worst-full bins and do some shopping.
It was a pretty warm day, the car's thermometer said it was about
100 °F outside, and the AC seemed a bit puny. It has a slow
leak to be sure, but more to the point it's hard to charge it properly
on a less-than-evil hot day, so I added some more refrigerant when I
got home. On the test drive it was getting 52 °F vent temps,
which seemed better.
I also noticed that one of the brackets holding the AC condensor in
was broken, probably from the dog incident. While it can probably be
welded, it's obvious that I'd rather not! I smashed up a wad of epoxy
putty and jammed it in there, we'll see if it holds. I don't want the
condensor flexing back and forth with vibration and inducing any
cracks in the operative parts.
Tuesday, August 16, 2005
The in-laws are in town, and this car's getting a workout since it'll
hold everybody.
Friday, August 19, 2005
My keyless fob had stopped working this car, but Jill's still worked.
As did the others, so it appeared that the keyless 'brain' had
forgotten its training. So I got out all four fobs and repeated the
training sequence. It's fine again. Weird.
Monday, November 28, 2005
Today turned out to be snow tire day. (It snowed last night.) This
was somewhat of an inconvenient surprise, as my wife needed to drop a
friend off at the airport in the early AM. My usual trick is to wait
until the day I wake up to snow, and then swap the tires before going
out. That didn't work today! She managed to make the trip OK on its
fairly new all-season Toyo's, but she did report some skidding around.
I did the swap after she got back.
Monday, February 27, 2006
Heard an intermittent noise from the blower that sounds like a leaf
stuck in it. I hope that's all it is.
Wednesday, March 15, 2006
My wife called me and said the instrument cluster was suddenly
inoperative, but that otherwise it was working fine. She suspected a
fuse and was worried about lights for her upcoming night driving, so I
dropped by where she was parked and checked it out. Fuse #6! Blown
solidly, with little black smudge. Odd, nothing seemed amiss
otherwise. She wouldn't have really missed anything on Fuse #6 except
the brake lights! I put in one of the spares and went on my way.
Thursday, April 6, 2006
I sat in the driver's seat for the first time in awhile today, and
immediately asked my wife "How long has the seat been broken?" It
lists to the left now, feels like a broken spring. She: "What do you mean?"
Me: "Didn't you notice it go 'poink' when you sat in it and
it dumped you to the left?" She: "Huh?"
I'm gonna have to dive into that before it pokes a hole in the seat
pad. I sure wish she wouldn't flop down into the seat the way she
does. Like a... no, I think I'd better not go there!
Friday, April 7, 2006
I pulled the driver's seat (what a PITA!) to find that yes, indeed,
there is a broken spring. Fortunately it hadn't poked too far into
the pad yet. The break was out in the middle where access would be
easy once the motorized frame was removed. While I do have extra
springs from the boneyard heated seats I procured (for the heaters, so
I can put them in our SL's), installing them would not be a quick job.
I decided that I could weld this break in place much easier.
To get the motorized frame off you have to be able to run it back and
forth to gain access to the various screw heads. If you pull the
plugs to the motors from the controller module you can see that two of
the five contacts are much larger than the others. These are the
motor connections, and it was an easy matter to hook a battery to them
to move them, reversing the polarity as necessary. The fun part is in
guessing which motor and plug is the one you need.
With the frame removed I laid old carpeting over the stump I use as a
welding prop and the ground, so that the seat wouldn't be scuffed, and
placed the seat for easy access to the bottom. Then I soaked a bunch
of old towels in water and laid them over everything so that only the
spring break (!) was exposed. That protects everything from flying
bits of molten metal. The ground clamp was secured to one of the
noninsulated crimps that hold the (coated) springs together. (I
theorized that the coating was penetrated by the crimped metal. In
fact it was.) Then I wedged the two broken ends together and hit them
with the MIG. Zap! The ends were secured. This, however, is an
insufficient fix as welding springs ruins their temper; I don't
believe that this kind of fix would hold long by itself. What I did
next was wrap the break in a bandage of mild sheet steel, a 1/4" strip
that had been cut out of another project. I then welded the wraps
together so that it is semi-solid. This, I hope, will hold it all
together. (I have done similar fixes before and none have broken to
my knowledge, but none have been subjected to
she-who-must-drop-from-a-height for any length of time.)
I put the seat on the ground and sat on it, and it felt better to me.
Reinstallation promises to be just as much of a pain as removal was.
But it's time for breakfast.
...As the seat was out I decided to try to do something about the
small tear in the bolster. It's gotten no worse in the years that
we've had it, so I have hopes that a repair will hold. I used big
wooden clamps to compress the bolster a bit, smeared contact cement on
both surfaces I wanted to glue together and let it dry until tacky.
Then I pressed the seam together. It held. I then got out the
leftover cream beige Leatherique dye and painted it on over the raw
leather. Looks pretty good, especially when compared to before.
We'll see if it holds up.
Reassembly of the seat was a pain. The seat can go onto the motorized
frame in two positions, one of them is not right. Believe it or not
the seat can be run an inch or two farther forward if you put it
together using the other set of holes. With enough fooling around I
got it back together and into the car. It took a couple of hours,
this is not a quick job. Much of the difficulty is because of the
motorized seats. Manual ones would have much quicker to deal with.
Tuesday, April 18, 2006
Long past time to take the snow tires off, finally got a chance today.
The changeover was uneventful.
Wednesday, May 17, 2006
As the day was hot (92+°F) I got out the AC gauges. The pressure
(and charge) was negligible, so I filled it, this looks like it's
going to be an annual (or semi-annual) event, at least until the leak
is identified and repaired. On a test drive the vent temperatures got
to about 51 °F, not great but acceptable.
After recharging the compressor was definitely cycling when set on
MIN, even though the vent temperatures aren't really that low. It may
be that the evaporator temperature sensor is a bit out of whack, I've
heard of this happening, but spot-checking it by getting a real
thermometer on there is not easy. (I'm told that overpressure can
also cause cycling off, so that might do it. The test refrigerant
tends towards higher-than-R12 pressures in this car.)
Wednesday, June 14, 2006
My wife called me from the road to announce that one of the wiper
assemblies had just flown off the car! She eventually found it in the
bushes and decided that it was missing the spring clip that holds it
in place. At my suggestion, she lashed it in place with a plastic
shopping bag, the flimsy kind. Great, we've got a road trip planned
tomorrow.
Tuesday, July 4, 2006
Cross-state road trip, 99+°F out there, AC on pulling a decent
grade and the engine temperature never beat about 110 °F; not
great, but passable. The AC was working very well the entire
trip.
Wednesday, July 12, 2006
On the way home we parked next to a well-used manual-tranny 240D in a
parking lot in Lake Chelan. Fun to tweak my wife by 'looking' at it.
On the grades up out of the hole to Waterville the car again pushed
110+°F engine temps, though the AC was not on at that time and
exterior temps were only in the mid-70's. Something in the cooling
system is marginal, I'm pretty sure it's the radiator. Still, the car
behaved well the entire trip, and even got 32 MPG on one leg over
back roads diagonally up from Long Beach to Roy. (Bracketing fillups
were in Astoria and Cle Elum, both sub-$3/gallon at Safeway stores.)
Got some interesting information on the electronic speedometer used in
these cars:
The heart of the speedo is an ITT UAF2115 integrated circuit. You can see
the whole datasheet for this chip at:
http://www.datasheet4u.com/html/U/A/F/UAF2115_ITT.pdf.html
MBZ uses a small generator (frequency proportional to speed) instead
of a circuit interrupter so there is additional circuitry to generate
the required waveform. The best coverage I found was at: http://cleanflametrap.com/speedo.html.
This link is actually for a 1991 120 MPH speedo but the circuit is
almost identical to my 1882 85 MPH speedo. The main difference was my
"setting" resistor was 59 ohms vs. 51 Ohms (connected between ground
and pin 4 or pin 7 of the IC). Note that the data sheet numbers pins
as if the 2115 were a 12 pin IC and the "cleanflametrap" link numbers
the pins like an 18 pin IC. Also, it seems some of the resistors may
be "selected" to tune the speed reading.
The mechanical part of the speedo assembly is impressive although mine was
quite different from the photos of the 1991 model. But both contain a
stepping motor that drives the odometer through a gear train and a separate
ammeter that indicates speed. Both are connected directly to the 2115 chip
except for electrolytic capacitor(s) across the ammeter that smooth the
current pulses because are too quick for the mechanical needle to respond.
So I replaced the shorted capacitor and the speedo needle now moves when I
spin the rear wheels on the jack stand. I'll road-test tomorrow and report.
Wednesday, August 2, 2006
Some notes I received on potential sources for replacement AC compressors
(not that I need one yet).
These cars have the 10P15:
- 82-86 Camry
- 85-87 Corolla
- Some Integra and 4 runner
- Lincoln prior to 91
I found a 10PA17C off a 90 Camry that I'd like to use. If I put the
SDL clutch on it, it looks like it is a bolt-up if I can find the
right manifold. The bolt spacing parallel to the shaft on a 10P is
about 2" while the same spacing on a PA is about 2-1/2" to 2-3/4" Since
both were used on MB, I think I should be able to come up with a
manifold.
I like the 10PA17 because it has a bigger displacement than the 15
and I think it might cool better at lower speeds than the 15.
I didn't think anyone else on the list would care much about all this
detail. I did get a 10P15C in case this experiment fails, and i also
have the option of cutting the MB hoses and splicing on the Toyota
hoses, since I got the fitting end of them also with the 10PA. If I
am successful in the end, I will try to write up what worked for the
list.
There are LOTS of 10PA in the PnP lot. Some look like they are in
good condition. All the 10P compressors I saw look like they are 20
years old and either dead, or subject to seal failure in the near
future. Looks to me that a 10PA conversion will give me a source of
cheap compressors for awhile. ($25 each)
Thursday, August 24, 2006
RF tire's leaking again. I took it off to find a nail in it, so took
it to Schwab where they repaired it. They noted that the tread is
about half gone, which is more than 50% of the life used up, and that
the tires will need replacing not too far off. I checked the records,
and the tires are 3.5 years old, with 46,000 miles on the car since
they were bought. (Some fraction of that on the winter tires.)
Saturday, October 7, 2006
Wife's been complaining that the keyless entry is not working (again).
Thinking that the system had again somehow managed for forget its
training I grabbed all four fobs and headed out to retrain it. Once
there I found that her fob worked great, the lights flashed and all
but the locks just didn't cycle. (They worked fine with the key.)
"Oh yeah", she says, "the lights work fine." Thanks for telling me
that to begin with, Honey! Anyway, I dug into the trunk and found
that the red wire to the keyless unit had corroded off of the resistor
that was inserted into the yellow line to the locks. Somehow there's
been water getting into the trunk well. I resoldered the wire back on
and the keyless system worked again.
I also noticed, and my wife subsequently reminded me, that one of the
rear door courtesy lights had fallen out of its hole and gotten
smashed when the door was closed. More to fix!
Tuesday, October 10, 2006
I glued together the pieces of the shattered courtesy light. It was all
there, except for the light bulb itself. (And the missing tab that had
let it fall into the door frame in the first place. I glued on a bit
of metal to take its place, I can bend it to fit.)
Wednesday, October 11, 2006
Scraped up another light bulb and installed the repaired courtesy
light. Ugly POS, but that doesn't matter, you can't see the lamp in
use anyway.
Saturday, November 4, 2006
The lashed-on windshield wiper blade finally fell off. I tried to
lash it back on, in the dark and the rain, but when it screeched on
the glass again after the first swipe we had to turn back and get
another car. I hope it didn't scratch the glass. (Driving in the
rain at night without wipers was pretty annoying.)
Later, in the garage, I could see that the lashing was just fine, the
problem was that the end of the rubber had come out of the wiper
blade, in the dark I couldn't see that. Anyway, tired of the lash-up
job anyway I drilled a small hole in the remains of the plastic clip
that had broken, and used a screw to pin the blade assembly to the
arm. It ought to stay put for an indefinite period of time, allowing
me to find a proper replacement.
Tuesday, November 14, 2006
My wife has reported that recently the keyless fob is no longer
operating the door locks, though it does flash the lights. I tried
the key in the trunk, and it doesn't operate the central locks either.
So, the pump has again gone insane. I power-cycled it and it began
operating correctly again. Apparently you just have to do this
sometimes.
While I was there I figured out why I can no longer lock the trunk via
the key: the male part of the auxiliary latch (an eyed tongue on the
trunk lid) is missing! It normally depresses a blocking lever out of
the way so that the lock pin can shift through the eye. With the
tongue missing the blocking lever prevents the pin from moving,
blocking the turn of the key towards lock. It must have dropped off
somewhere along the line, I've not seen any extra metal parts around
here or in the trunk. There is a paint outline on the trunk lid, we
certainly used to have one. It may be that the body shop lost it, and
I've not really noticed since then. Will just have to get another one
from the junkyard (easy, but time-consuming), or dig into the rear
trunk wall to remove or disable the extra latch (more difficult).
Tuesday, November 21, 2006
We swapped cars today, and while driving this one I noticed a weird
little creaking coming from up front. Last time I heard something
like this I'd finally figured out that it was the hood rubbing against
its rear hold-down pin. I cleaned and lubricated these pins and the
mating surfaces, we'll see if that does anything.
Saturday, November 25, 2006
Snow tire day.
Tuesday, December 26, 2006
My wife has been complaining of the brake pad lamp coming on
intermittently, so we ordered new pads and sensors from Rusty over the
phone while on our Holiday road trip. They ought to be waiting for me
when we get back home, then I'll just have to make time to do it.
Monday, January 8, 2007
Installed new brake pads and sensors. Only one of the sensors had
been nicked, it looked like there was probably about another year on
the pads before they started scraping. Nonetheless, it's done. The
brake fluid was nasty, so I did some bleeding while I was there. (You
pretty much have to in order to prevent overflowing the reservoir when
you push the pucks back to put new pads on.) I didn't have time to do
a thorough job. The rotors are definitely ridged, probably next time
they'll need replacement.
There is also something loose in the right-side tie rod business. By
eye, I'd guess either the drag link or the idler arm. Will need to
look into that soon. Maybe when it warms up a bit.
The power steering fluid was again out. I really need to track down
that leak and fix it!
Friday, January 19, 2007
My wife has been complaining of the cold draft coming up the shifter
due to its torn rubber boot. I opened the console to replace it with
the new one I had procured some time ago for my SL, only to find
(besides everything all being kind of glued together with spilled
coffee) that the part, while close, is too small. So, the
correct part's on order and the car, though driveable, is in a rather
ugly state. I didn't put it back together, in order to save myself
some work later.
Saturday, January 27, 2007
The new shifter boot came yesterday, so I installed it this morning.
Ought to shut my wife up, who's been complaining about the inability
to run the windows. Who wants to do that in below-freezing weather
anyway? But I forgot about Starbucks' drive-throughs. Silly me.
Had some trouble reinstalling the shifter gate, and managed to damage
its mounting ears. On top of that, in spite of my checking before I
buttoned it up, its lamp is out so I have to open it up again.
Sigh.
Sunday, January 28, 2007
Replaced the stupid shifter light bulb. It's actually pretty easy,
all you have to remove is the ash and storage trays. Two screws.
Don't even have to lift the wood shifter surround.
Thursday, February 8, 2007
My wife has been complaining that the keyless entry isn't working
again. I looked, and the wiring is again puddled in water and
corroded away. I fixed it. Again. I don't know how many times I
have to tell her that the trunk seal does not work well, and
I doubt it can ever be made to work well. (The car has been hit in
the rear at least twice, the body shop work is adequate, but not
great. I have worked on that seal many times, it just won't seal
well.) You can't take this car through an automatic car wash
without filling the trunk with water. Yet that's what she does.
Regularly. And she's always so proud of how clean it is then...
I dried the spare tire well, and cleaned out the drain holes. (The
drain works, but that doesn't mean that water doesn't slosh around in
there some. The drain has kept the keyless module and the door lock
pump themselves from flooding, but the wiring still gets wet.)
Saturday, March 15, 2008
I took the garage door opener out of this car (it was clipped to the
back of the under-dash panel, on the top side) and put it into the 190D, then swapped the cars, so that this car is
now in the new garage center slot (the operating theater). It started
easily enough, but ran really rough and smoky for a minute or two. I
think I need delivery valve seals on the injection pump. It's also
very oily all over, it needs re-sealing. And then there's the rest of
the laundry list...
I found the beginnings of a mouse nest in the trunk, along with a huge
pile of D-con poison. I also found a dead mouse under the car.
I don't think there was serious damage yet.
Thursday, March 20, 2008
I traded a good courtesy lamp for the broken and glued-together one
that was in the left rear door. (The crappy old one is going to be an
auxiliary trunk lamp in the 190D.)
Friday, November 7, 2008
Score! The U-Pull had in a 300SE, so I dropped by, even though the
weather was miserable, with heavy cold rain. It had one rear
taillight lens in excellent condition, now mine for $6. I also got
its auxiliary trunk latch tongue, which this car has been missing for
some time, and the two rear reading lamps (with the expensive bulbs)
for $1 each. I also got one exterior heated mirror, for $7. They
also had a 280SE (116) and it had its complete toolkit, though very
rusty and the roll was rotted. That was free.
Monday, December 14, 2009
I swapped the Hakkapeliitta 1 snow tires to the SEL. Twice as much work that way!
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