Log of the E320 #2's life with us.
Monday, December 31, 2018
I stopped by the lot to look at the car. Turns out they weren't open,
but I could see it, took a walk around. Was decent looking, not all
bashed up. Worth coming back, they re-open on Wednesday.
Wednesday, January 2, 2019
Lot owner states that they can sell all of these that they can find,
quickly, and buy them when/wherever they notice one for sale. As in:
don't dick around, it won't be here long. (He even mentioned a
bounty, if I knew of any for sale in the wild.) Well, that may be a
sales pitch, but it's probably fairly true nonetheless. Took a test
drive, noticed a number of problems:
- Fob doesn't work. (They say it has a bad vacuum pump, and
provided a used one in a box. So, door lock, trunk, and headrest
release systems are not functional. Trunk will only open with the
emergency key.)
- LR interior door handle not working. Feels broken inside.
- Lamp behind the warning center is out.
- Dead pixels in side LCD displays. (Extremely common, and a
straightforward fix.)
- Dome lights don't come on with doors. (Turned off with switch,
bad/misadjusted door switch?)
- Driver's seat heater seems inoperative.
- Squeaky/jiggly ride. Probably needs new shocks and struts.
- Only one key. Spendy!
- No fog lights.
- Squeaky roller on passenger-side seat belt.
- Rear-seat cupholder stuck.
- Tear in driver's seat bolster. Looks almost like a cut rather than wear.
Bought the car, settled on $2,500 as-is. Weighed in at $2987.75 with
all the fixin's. They say to call them if/when I need parts, as they
have an excellent deal with a wholesaler.
Filled up car. Wants premium, it got mid-grade.
At home I bought an owner's manual set on eBay: $27.19
Thursday, January 3, 2019
I pulled the rear seat bench and removed the PSE (vacuum pump), and
installed the replacement. The door locks and trunk work again, but
there is apparently a leak in the passenger front door pod, because
the pump can't quite make it actuate by itself, and the lock howls a
bit during the procedure. If you assist this plunger in its travels
the rest of the car follows suit and the pump turns off. A leak such
as this apparently can destroy the pump motor due to running in vain
for too long. This will have to be addressed before the car is ready
for use. (Looks like both the RF and LR door panels will need to come
off during this sort-out.)
The original pump is 210 800 19 48, but the used
replacement that came with the car is 210 800 11 48.
The former apparently supersedes the latter. A new pump is
about $650, and a rebuilt one is $450! Burned-out motors due to
vacuum leaks are apparently the common failure.
I noticed that the driver's seat heater fuse was missing, so I put in
a spare. We'll soon see if it's missing for a reason.
Friday, January 4, 2019
At lunch I spent an hour on the car. I opened up the RF door panel,
it comes off fairly simply:
- Pry out two plastic plugs, and the handle bezel, and remove the three
big Philips-head screws thus exposed;
- Remove lock knob, run down the window, and pry up the top cover, out
of the four metal clips that hold it in its channel;
- Remove the door striker trim, and pry out (carefully!) the plastic
pop-rivets that hold the panel in place.
You can then unplug/unhook the lights and the seat switch connections
to the door panel, and set it aside.
With the guts thus exposed you could hear the door latch leaking when
you tried the fob. I unplugged the vacuum/pressure hose and taped
over it, thereafter the rest of the car locked and unlocked with
alacrity. Time for a new pod? We also need a plastic pop-rivet or
two, they haven't all survived 'til now in good condition. I put the
door latch bezel back so that the courtesy lights function correctly,
as it's what depresses the switch in the door frame at the B pillar.
I put the lock knob back so that the door can be operated
semi-normally while I await parts.
I went around to the other side and removed the LR door panel, same
procedure. The problem there is that someone had clearly been in
there, and had not correctly reassembled things. The release cable
had popped out of its eyelet on the handle. The trick there is that
the cable body has to be clipped into the door panel, which you do by
'opening' the door and slipping just the cable (and not the sheath)
into the slot provided for it. Reassembly is just the reverse of
disassembly. After that the door would open correctly from the
inside.
Finally I tackled the driver's door courtesy light switch.
Examination in daylight showed that the door itself closed properly,
and that the latch bezel was correct. The problem is that the switch
body had been punched in a bit, and sank into the frame under its own
spring pressure enough to prevent the switch from opening. I just
removed the switch, thereafter the courtesy lights could be re-enabled
via the overhead switch, and all seemed to work properly.
I need to order:
- Door lock pod, P/N 202 720 44 35;
- Door panel plastic pop-rivets, P/N 011 988 76 78;
- Door switch, P/N 202 820 94 10.
That door lock is $250! The vacuum part is not separately available.
I ordered the other parts from FCP Euro, for $13.70. (Four panel
clips and one door switch.) I'm going to be examining my options
here.
Saturday, January 5, 2019
Daniel and I went to Pull-and-Save, they had a couple of newer cars
there. I managed to drop about $40. From the E320 I got the door
latch. $2! Its courtesy light switches were an older style, and not
usable. From the slightly newer C230 I got a courtesy light switch
that fits and works; I installed it in the parking lot; $3. I also
picked up its Owner's manual. It's older and not particularly
accurate, but is better than nothing and does cover the climate
control system; $2. I also grabbed a handful of dash lamps and some
fuses from the C230, they look like the kind the E320 uses.
The bad right front door latch was there on the E320, and its locking
diaphragm was intact. (You can test this by corking it with your
thumb while you move the locking knob.) Thus began the nightmare!
That SOB does not want to come out, it's trapped behind the
riveted-in window guide rail. The main problem seems to be the molded
plastic rain guide, which is snapped to the latch. If you can figure
out how to separate the two first, then the body of the latch can
pivot around the window rail and come out. That took us maybe 40
minutes to get out. I also grabbed some plastic pop-rivets for the
door panel.
Daniel was whining because his seat was fully forward on the trip in,
from my earlier work in the back seat, and the switches were at home
on the door panel in the garage. I spent $9 and bought the E320's
door switches just so that he could adjust it better for the trip
home. I'm so nice! They can go on the spares shelf, I guess.
At home the nightmare really began. First we had to get out the old
door latch, which was, if anything, worse than the first one. In part
because I cared more about not ruining anything. The bad
latch was P/N 202 720 44 35. The older latch from the
yard was P/N 202 720 20 35, and was set up for a
mechanical key lock. It looked, however, like it would fit in place
of the simpler lock-less one. Getting the thing put back together was
a nightmare. The biggest problem was getting the latch back in place,
and the handle on, all while not losing the screw that holds the
external (infrared?) lock plate in place and making sure the connector
to that piece was in place. We lost that screw into the door guts
twice, and had to take it all back apart and fish with a magnet to get
it back. Frustrating, and time-consuming. However, eventually we
prevailed, but we really did need four hands and two sets of eyes to
get it done. (This would likely not be necessary for somebody
experienced at this, who knew all the tricks.) This consumed a good
three or more hours, total.
Once it was somewhat together we tried out the door, including the
locking system. It all seemed to work nicely. I was too tired to
finish putting the door back together, and it was starting to get
dark. Tomorrow.
This particular door latch seems very poorly designed, an all-in-one
monstrosity that may be quick and cheap to assemble at the factory, but
which is a nightmare to service in the field. The part, bought new,
is quite expensive. Smells of cost-reduction to me. (To the factory,
not to us!) Three separate parts, rain shield, latch, and vacuum pod,
which would be infinitely easier to service, and cheaper, as
separate parts.
Sunday, January 6, 2019
We were planning to go to the boneyard again, to try to liberate some
parts for the 190D, so I decided it was time
to fabricate some dash cluster removal hooks; I used welding rod. (To
get the boneyard 190E's cluster out, as well as this car's.) I spent
some time making a T-handle with a hooked end, using 3/32" rod.
The worst part was trying to weld the handle end into a unit so that
you could pull from both wings of the handle without it bending to the
side. (I burned through several of these fabrications until I got the
heat on the wire feed dialed in.) In an effort to make it stronger I
used the smoke wrench to heat the hook end red hot, then quenched it
in some ice that was laying there. I made two of these, and found
that 3/32" rod is simply not strong enough, the shaft bends so
that the hook comes undone when you pull hard on it. I made one more
with 1/8" rod, and was able to use it to pull the cluster out of
the E320; in spite of the extra thickness of this rod I was able to
find spots to wedge the hooks in. (The same was true of the yard's
190E, later in the day.)
With a rather distressingly hard pull the cluster came out. I
unhooked the two electrical connectors and removed the cluster from
the vehicle. I replaced the two burnt-out 1.2W (green base) bulbs
with two of the 1.5W (cream base) bulbs I got at the boneyard
yesterday, I trust that this will do until/unless I get the correct
lamps. I put the cluster back, but did not push it into place as I
still need to go over all the lights, and also cure the LCD
display contact issues. After this the odometer and warning center
display was nicely visible, if perhaps slightly bright.
At the boneyard I bought the 'wrong' vacuum pump from their E320. It
had occurred to me that while the assembly was definitely wrong, the
motor inside, the part that is reputed to fail most, is probably not.
$13. I also picked up two E320 wheels, for possible snow tire duty.
Those were surprisingly expensive, $16 each plus $15 each for
core charge, and they don't really match the style that is on either
E320 we have. (I'll see if I have something ratty around here to
return for cores.)
On the way back home I stopped at the FLAPS to replenish my glue
supplies, particularly the 3M spray 77 glue I use for door moisture
barriers. They had a thermostat for this car on the shelf, $32. (It
comes with an aluminum housing, which seems odd.) I also bought some
G-05 coolant for the job. The car's been running at about 60°C
indicated, which is low; it should run at 85°C.
Monday, January 7, 2019
At lunchtime I went out and glued the vapor barrier back to the door.
Putting the door back together, I had a couple of the attachment rivet
mount points come unglued from the panel. I used weatherstrip cement
to re-glue, because I thought it'd dry faster than Shoe Goo. I don't
think it's really strong enough, next time that door comes apart I'll
probably re-glue with something better. Anyway, with some fiddling I
had the door back together, and the rear seat back in. Looks good!
I found one extremely corroded chrome-plated aluminum bundt wheel to
return for core charge. Need to find another useless/ruined wheel to
return... (There's a $5 charge if the wheel is encumbered by a tire.)
Thursday, January 10, 2019
The owner's manual set arrived. Hardback! It's in a nice folding
pouch, but did not come with a COMAND manual, bummer.
At lunchtime I tackled the malfunctioning license plate lamp.
Apparently post-'facelift' this can no longer be done easily,
requiring the trunk lid liner be removed for access. (Security? Were
people able to pop the trunk by removing the license lamps from
outside?) That was a pain. It seems like it wasn't the bulb, but
some kind of loose connection, I'm not sure that it is
permanently fixed, I guess we'll see.
The fog light fuse is intact, so that's not the problem there.
I found that the blue base 1.2W bulbs from earlier cars seem to fit
well enough in the instrument cluster, and work. These bulbs don't
protrude as far into the light chambers as the green-base bulbs,
resulting in a bit less light, but I think it'll be fine. Beats
ordering (and paying for, and waiting for) exact
replacements. I also pulled open the instrument cluster and tried the
'increase the pressure on the LCD ribbons' trick, along with a dusting
of De-Ox-It. No joy. New ribbon cables are available online, as are
replacement LCD's with cables, at moderate prices. I may just try
'replacement' with the cables that are there, after a full cleaning.
Seems fairly involved, and fiddly, but the price will be right if it
works, and there are reasonable Plan B options.
Friday, January 11, 2019
I opened up the instrument cluster, with an eye towards refreshing the
LCD ribbon cables. What was not clear from all the online
instructions is that the act of peeling them loose from the PCB's and
LCD's destroys them. It is possible that acetone might have allowed
their release and re-use, I don't know. Maybe next time,
on Barney? What is clear is that I now
need new ribbons before this cluster can be used again. (In a pinch I
could re-assemble it to use while I waited for parts, but then I'd
just have to take it apart again.)
Saturday, January 12, 2019
I had a look in Barney, and it had the cupholder
mechanism in one of the two consoles stored in the trunk, fully
functional. (One console is broken, the other is intended to be the
replacement.) I stole the cupholder mechanism, cleaned off the
spillage goo with hot water, and installed it. She'll need it far
more than I ever would. (I still may need to remove the entire console
in order to repair/replace the wonky cupholder cover mechanism.)
Thursday, January 17, 2019
The new instrument cluster ribbon cables came today. I looked up one
of the conductive glues used in the industry, and the 'soldering' spec
is 180°C for 5 seconds, at 3 MPa of pressure. I have a
temperature-controlled soldering station, that looks like just the
ticket.
Friday, February 15, 2019
I picked up the license plates today. They had a 2000 E320 4WD wagon,
silver with 199kmi going up for sale. Price mentioned was $3,300-ish.
They offered me a finder's fee if I threw them a buyer.
Sunday, March 10, 2019
It's been far too long, and we could really have used this
car in the last month. I used acetone and swabs to clean off the LCD
displays and the circuit board, and 'soldered' the new ribbon cables
on at 180°C. I partially reassembled the instrument cluster and
put it in the car. The operation was not a success, there were many
bad segments in the display. (Better than before? I'm no longer
sure, it's been too long.) Unfortunate.
Saturday, March 16, 2019
I installed the dash cluster, and used a potato fork to chip away the
ice berms behind the car so it could actually back out of its hole.
(It couldn't reverse out of there, 4wd or no.) With the car out into
the open, I installed the license plates and the new thermostat. The
license plate screws were very corroded and stiff, I used a
M5×0.8 tap and die to clean and lubricate the threads, which
made putting the plates on much easier. The thermostat job was
delayed by my losing track of where I had put the new E sockets, and
losing one of the two thermostat bolts down onto the plastic engine
pan. I had to jack up the car and remove two of the pan mount screws
to liberate it. Otherwise, the job was very straightforward. I
buttoned it back up and topped off the coolant with fresh G-05. I
used the usual trick of removing the radiator end of the upper hose,
pouring coolant in to the tank until it began to spill out the opened
hose, then pouring into the joint between hose and radiator until I
can't get any more to go in there, then ramming the hose on and
tightening it. This burps out most of the air, making the whole
process a lot more certain.
We went for a test drive, it was sunny and near 50°F so I opened
the sunroof. The car warmed up to just over 80°C indicated, so
the thermostat (a Mercedes original, 112 203 02 75) was
indeed at fault. The attempted repair on the LCD screens made
it better than before, but it's not good yet.
I took one ratty alloy wheel back to Spalding's, to reclaim
the core charge. I haven't been able, so far,
to find another ratty wheel lying around, I thought I had one. They
were a bit snotty about how long it had been since I bought the wheel,
I may end up eating the other $15 core charge. At least that garbage
is now out of my trunk. At Spalding's I checked the coolant level, and
it was still good.
Monday, March 18, 2019
I drove the car in today and had the sellers scan the codes, as the
Check Engine light has been on. Their Maxi-DAS came up with:
P0115 | Engine Coolant Temperature
|
P0410 | Secondary Air Injection System
|
P1747 | Electronic Pressure Control
|
This might be semi-spurious, so I had them clear the codes and we'll
see if anything comes back.
Friday, March 29, 2019
The P0410 code is back. Brother suggests that it's possible the check
valve is leaking backwards a bit, causing it and/or the air pump to
get corroded inside, causing this kind of problem. It needs a laying
on of hands.
Wednesday, April 3, 2019
On the recommendation of the seller I called On-Site dash repair
regarding the LCD problems, and it turns out they don't do this
themselves, they'd send it off. They quoted $275–325, depending
on which exact model it was. Not too attractive, at that price I can
afford to take another stab at it myself.
Saturday, June 1, 2019
I ordered front shocks for the car. $346.98, with bellows, for the
correct Bilsteins from FCP Euro.
Sunday, June 9, 2019
The shocks came a few days ago. I put the car up on ramps, and had a
look. Looks straighforward... NOT! I did some more Googling, a bit
more thoroughly this time, and it looks like this is actually a bitch
of a job, requiring ball joint and half-shaft removal. And, the fancy
Klann spring compressor I own is not the correct tool for this job.
(You need a different Klann compressor.) Perhaps I should
just cave in on this one?
Tuesday, June 11, 2019
I called around. The usual places (Silver Star, C&H) would not
install the $350 worth of parts I had already bought. European
Autohaus (Thorpe Rd.) would, for roughly that same charge, but with no
warrantee on the parts. Good enough. I made an appointment for
Wednesday the 26th.
Wednesday, June 26, 2019
Dropped the car off. They think it'll be done today.
It was. They said, though, that the front CV boots were shot on the
passenger side.
Thursday, August 15, 2019
Loose flat on LR. Local Schwab said it had a sidewall hole,
non-repairable, and had circled it. I couldn't see anything. Today I
took it to a different Schwab, they thought it was flaking chrome on
the wheel's seating surface. He wire-brushed it and put in a new
valve stem, just to be sure.
Thursday, August 29, 2019
Silver Star Automotive quoted $873 to reboot, vs about $60 more for a
new aftermarket axle. Not very attractive.
Tuesday, December 3, 2019
The LR flat has been getting worse, it now requires a daily airing up.
I took it to Liberty Tire, and they were unable to find the sidewall
hole. (I had seen the leak myself, so it wasn't imaginary.) They did
find a bit of metal in the face though, and patched it. We'll see if
that takes care of the problem or not. They gave me a piece of chalk
and told me to mark the leak and bring it back, if I saw it again.
Monday, December 23, 2019
I saw the tire leak in the rain, and marked it with the chalk. It's
in the round mold mark in the tread over the "E" in
"GOODYEAR". No time to do more than this, however.
Tuesday, January 7, 2020
I finally had a chance to take the car back in, now that things have
stabilized after the holidays, and they have supposedly fixed the tire
leak. No (additional) charge.
Monday, June 22, 2020
Jill took the car to go visit her Dad for Father's Day, and on the way
back, a mile from home, it died. She pulled off safely, and the car
would crank but not start. We towed it home, the chances are good
that the crankshaft position sensor (CPS) has died. Good thing she
was so close to home!
Wednesday, July 1, 2020
I gambled and took the car to Silverwood. Well, I tried, and lost the
gamble. It made it as far as Rathdrum before it crapped out. I
called for Daniel, and he and I towed it home on a rope. It would
run, briefly, after a cooldown, but wouldn't run long after that. I
had come prepared with the cheapo OBD-II reader, and it showed codes
after the no-start: P0410 (the persistent air pump code), P0300,
P0304, P0305. The three new codes are, respectively, random misfire,
cylinder #4 misfire, and cylinder #5 misfire. According to lore these
can also be caused by a failing crankshaft position sensor (CPS), even
though there are dedicated codes for that that were not thrown here.
Certainly the symptoms exactly match common CPS failures.
I looked into ordering a CPS, but there are too many different ones
that it might be. Advice was to pull it and order another of whatever
came out. I peeked, I can't see it, though it's supposed to be on the
driver's side of the bell housing, up front and high.
Thursday, July 2, 2020
Yesterday's episode really drained the battery, Daniel had the key on
while being towed home so that he had wipers, signals, etc. It
wouldn't crank once we got it home. I put it on charge, it drank long
and hard. I used my recent garage-sale find, another old-school
Schauer automatic charger like the one I've been using for decades.
Friday, July 3, 2020
I felt around and found the CPS by Braille. Once you know exactly
where it is you can see it, sort of, if you contort yourself just
right while crouching on the engine. It unplugged easily, but getting
it out was another story. It does use an E8 external Torx screw. The
secret was a 1.5" 1/4" socket extension, my 1/4" E8
socket, and a small 1/4" ratchet wrench. That extension was long
enough to clear the CPS itself, but not so long as to push the wrench
into something else. Other suggestions involved a 1/4" knuckle
and long extensions, but this actually worked much better than long
wobbly bits would have. (I tried to do that, briefly, before I hit
upon using the very short extension.)
The CPS was very oily, and is Bosch 0 261 210 171,
Mercedes A 003 153 27 28. I ordered one from
Amazon, about $28. I used Jill's account, to get the free Prime
delivery.
Tuesday, July 14, 2020
We determined that the replacement CPS must have gotten caught up in
packing material and discarded by accident, so we've ordered another
one. Delivery was claimed, as part of one of Jill's orders, but she
doesn't remember ever seeing it. Unfortunate.
Friday, July 17, 2020
The CPS came yesterday, this morning I installed it. It's easy, once
you know exactly where it is and what you are doing. I used some
DeOxIt on the terminals, just for luck.
While I was there I hooked the battery charger to the secondary air
pump. Drew 6+ amps, sounded like it it was working fine, not sure
what to make of that.
Wednesday, September 2, 2020
On the way to Long Beach the front belly pan blew down and started
scraping on the freeway, making a horrid noise. I pulled/cut it off
and put it in the trunk, and we continued on our way.
Monday, September 21, 2020
Jill's starting to drive this car more. I taught the embedded garage
door opener what to do. Just like the X5, it couldn't see the Wayne
Dalton remote at all, so I taught it the auxiliary remote opener
control I installed some time ago. (This was made more difficult
because the auxiliary fob's little 12V battery was dead. I had to
jumper a big lead-acid battery to it to make it work.) Like on the
X5, this may or may not work well.
Tuesday, September 22, 2020
We tried the embedded opener, and it seems to work fine. Better than
it ever did with the X5.
Monday, September 28, 2020
Dropped the car off at A&B Motors. Their estimate of the axle
repair was half that of others I'd gotten in the past.
They called at about 2PM, said it was ready.
Tuesday, September 29, 2020
Picked up the car. $487.33 for the axle repair. ($185 for the axle,
$250 labor to install. Plus tax and shop supplies.)
Wednesday, September 30, 2020
I mailed off the instrument cluster for LCD repair, to MVKMimi1 in
Littleton, Colorado. (odo-pro.com) $107.02, order #02-05818-02558.
Plus almost $20 in mailing costs on my end.
Friday, October 9, 2020
The cluster came back today, but when I installed it in the car it was
inoperative, claiming "display defective, visit workshop" or something
like that. No activity on anything except the clock, no gauges
moving, white field for the gear display, etc.
Saturday, October 10, 2020
I took the cluster back out to document exactly what it said for the
bitch-o-gram, and it decided to work instead. WTF? It's a lot colder
and wetter today, could that have been it? Some research suggests
that there are a number of innoucous things that can cause that
message. This was suggested:
The fault you describe is either the washer bottle level sensor or
coolant level sensor that is defective. They are wired in series and
work on a voltage coded system read by the instrument cluster. If the
voltages are not within its parameters it gives this display. No
guarantees which one but odds on it's the washer level sensor.
Tuesday, October 13, 2020
According to the online tire selectors, the correct snow tire for this
car is the Nokian Hakkapeliitta 8 or 9 in 215/55R16. Or, a 195/65R15
if a 15" wheel will work. (Four listed sizes for this chassis
from Nokian: 195/65R15, 205/65R15, 205/65R16, and 215/55R16.)
Discount tire is now listed as a Nokian dealer.
Wednesday, October 14, 2020
The dash had illumination problems, and I found two dead bulbs. I had
a spare 2W push-in bulb for the main cluster lighting, but I couldn't
find my spare colored-base twist lock bulbs. However, I can live
without the seatbelt warning lamp, so I switched it for the dead
illumination lamp on the main LCD display. It all looks good, now.
I checked out the seat heaters. This system uses only two wires, the
two heating pads are in parallel and are PWM'd for the low heat
setting. (Some systems put the two pads in series for low, and
parallel for high.) The power goes into a 2-wire plug at the front of
the seat frame, the one with heavy wires. The socket has four spade
contacts on the seat frame, the two pads are in parallel at that point
due to the way the plug is wired. The pads are about 2.5 ohms (60W)
each on the passenger side, which does seem to work. They're both
open-circuit on the driver's side. Both sides get power when the dash
switches are operated.
So, just about what you would expect. The heating pads on the
driver's seat are both broken and open-circuit, and probably require
complete seat removal and disassembly to correct.
Joy.
Friday, October 16, 2020
More research on the seat heaters suggests that the W210 does not use
separate heating pads, but rather a serpentine wire laid into the foam
padding under the seat covering. This gives a much wider heating
profile, encompassing the bolsters as well as the center sections, but
is also more fragile. These wires seem to break on the outer
bolsters, which are high-stress areas. OTOH, it is apparently often
easy to repair the breaks in the wires—once you get access to
them!
This promises to be a slow repair, which is not too cool if you want
to be driving the car. I wonder if I can get a spare seat to swap
into the car in the interim? How hard is it to remove a seat? Looks
like it's pretty much the same as on older cars, but uses an E12 Torx
rather than a hex-head bolt. In the junkyard, the lack of being able
to move the power seats will likely be the major sticking point.
Sunday, October 18, 2020
Yesterday I hit both cheap junkyards, but there was nothing I could
use. Today I tried one of the 15" 124 wheels I had in the
stockpile, but it wouldn't go on over the (front) brake caliper. So,
we must use 16" wheels, of which I have only two. Also, there's a
sidewall bubble on the LF tire, so that will have to be replaced.
Stupid 17" wheels and their weak-ass low-profile tires.
I started checking Craigslist, and found a W210 car being parted out.
Turns out it had been stripped of 3 of the wheels, but one was left on
it and there was still one in the trunk. Somewhat weird acquisition,
a bit sketchy, but ended up with the two 16" wheels for $20.
They're not an exact match to the other two, but they're close in
style.
Monday, October 19, 2020
I checked around, and Discount Tire (local) could get them in for $180
each, in 215/55R16. Hakka 9's, studded. Probably about $900
installed. They'll call when they're in, they had to order them.
Monday, November 9, 2020
They never called on the tires, but I dropped by today and they were
actually ready. Looks like they had been for a little while. The
tires are directional, and there are two different kinds of wheels.
I'd requested that they make the lefts and rights match, but of course
they did not.
Thursday, November 12, 2020
I put the snow tires on. The two rear tires that came off have very
low tread. The fronts look very good, except that the driver's side
has a sidewall blister. Probably time for new tires to go on in the
Spring, with one good take-off.
Saturday, November 14, 2020
I removed the driver's seat, and peeled the seatback cover off. Not
Easy. The hardest part was unclipping the plastic hooks that pull the
cover (via heavy wire sewn into the cover) back against the pad and
springs. (I also broke the plastic headrest sockets, as I couldn't
see how to get them to release.) The broken seat heater seems to
start with a fine braided copper wire, looking something like solder
wick, molded into the foam, which morphs at some point to a thin (30+
gauge) blue insulated ultra-fine tinned copper stranded wire that
weaves throughout the foam in the back. (The blue insulation is thin
and tough, reminding me of wire-wrap wire rather than the usual soft
PVC.) Peeling back the bolster where the cut in the leather was, I
could see where the wire was broken in that area. Only one side had
continuity to one of the terminals, which means there is more than one
break. Great.
The design is bad. While the serpentine wire is closer to the human
body, and thus can provide heat quicker and over a larger area than
the older separate heating pads, it's very vulnerable to damage, and a
poor design choice for long-term reliability. I think that only the
W210 used this kind of design, and they went back to separate pads in
subsequent models. I think that if they'd used wire of twice the
gauge, and twice the length, that it would have held up to the
physical stress much better.
Sunday, November 15, 2020
I chased the wire around the offending outboard bolster, using a razor
blade to cut through the felt and into the foam, working the wire out
of the pad, and found all the breaks. Cutting out the bad spot and
soldering the ends together works well. I had one break to repair,
and one accidental cut. After that the whole panel had continuity,
and seemed to heat well when hooked to the (larger) bench power
supply. I'm running a 5A test current. I used duct tape to secure
the wire back into the pad.
While it was 'burning in', I turned the seat cover inside out at the
tear (that was over the heater break) and got the lips of the tear
closed up. I used duct tape to secure the face into position, then
cut a piece of chamois cloth (leather-like, tough, water tolerant) to
cover the tear. I used black weatherstrip cement to cover the
chamois, then pressed it into place over the tear on the back side. I
then sandwiched the repair between two small anvils to press it flat
while the glue dried.
During all this the current through the heater became intermittent,
chopping in and out, and gradually getting worse. Arcing? Eventually
it failed altogether. Not Good! This does not bode well for a
semi-permanent repair.
Monday, November 16, 2020
The tear repair looks pretty good, I guess we'll see how (if?) it
holds up with time. There is a worse tear at the piping of the side
seam that I still have to figure out what to do with.
I began chasing down the new break in the heater. The problem lay
between the two repairs of yesterday, in the high-stress bolster, so I
began cutting more wire out of the pad between them. I eventually
found a slightly discolored place that seemed to be the new break. I
cut it out and stripped back the ends and soldered them. (The wire is
embedded in a wavy pattern, so it's easy to get a little slack to work
with.) Once repaired I could again apply the 5A burn-in current,
we'll let it cook for the day.
I then tucked the heating wire back into the channels in the foam and
used little strips of duct tape to tack the channels back closed. A
layer of duct tape over the whole thing completes the repair. I then
turned on the current for another burn-in.
Next is to see what I can do about the other tear in the upholstery,
where the seam failed at the outside piping. I used black
weatherstrip adhesive to tack it closed, using small spring clamps to
secure it while it dried. This is only a tack step, I plan to secure
it from behind somehow.
...by late afternoon it looked like the current was beginning to
fluctuate again, and by evening it had burned out again. Still not
done!
Friday, November 20, 2020
Road trip tomorrow, and the seat isn't done. I stole the driver's
seat from Barney and put it in (temporarily).
It doesn't take long to do this. The seat heater even seems to work!
Wednesday, November 25, 2020
Yesterday and today I got back on to the seat repair, and got the
tears mended. I glued more chamois across the seam tear, and clamped
it into place. In several sessions, in order to get it well secured
on one side before gluing it across the split seam. It looks pretty
good, and I hope it will be strong.
The next seat heater repair promises to be unpleasant, continuity
tests show the latest break is not where the other ones were.
Thursday, December 24, 2020
I ordered a replacement hood star, $16.74 from China, Inc. Probably
will take a month to get here.
Monday, January 11, 2021
The hood star came Saturday, and I installed it today. It's really
easy to do, just a 90-degree twist lock on the base. The star looks
good, not flimsy or anything. The base mechanism is slightly less
robust looking than the original, but not likely to be any kind of
problem.
Sunday, April 4, 2021
The rear cupholder was sticky enough that almost breaking force seemed
to be necessary to get it to extend the first time we used it on
Thursday. I figured out how to remove it (pull it all the way out,
exposing the first-aid kit tray, then flex the center bottom of the
tray upwards to release the catches and pull it the rest of the way
out). I could then give it a warm soapy bath to remove all the
spilled residue.
On a roll, I then liberated the fancy front cupholder. It had gotten
to the point where it would not stay down. Only some modest pulling
was necessary to get it out, whereupon it got the same soapy bath
treatment. That freed up its catch mechanism. I then mopped out the
well, getting a lot of spilled residue out as well as some corn chips.
(Ugh.) The door cover seems to be working better now, too. At this
point they both work about as well as could be expected.
Sunday, April 11, 2021
I ordered an open-box Curt 11744 hitch, for use with a bike rack.
$140 with tax via eBay.
Saturday, April 17, 2021
I ordered a used, lightweight, 2-bike carrier for a 1¼"
receiver, via Amazon—$38.35 with tax and (free) shipping. That
should work better on the car than our heavier carrier, which would
also need an adapter to neck down the stinger.
Tuesday, May 4, 2021
Daniel and I installed the hitch and bike carrier today. That
was not particularly easy. Steps:
- Remove trunk interior lining, both sides and back. Many pop-out
plastic wedge clamps, screws, etc.
- Remove bumper cover. 6 screws and 3 nuts.
- Locate hitch, mark hole centers, drill 8 holes. Paint hole edges
to prevent rust.
- Bolt on hitch.
- Put back bumper cover.
- Put back trunk lining.
Complications were numerous:
- The online instructions we found for bumper removal were totally
inadequate. Only 3 nuts my ass.
- The plastic pieces had been broken in places already, presumably
by earlier ham-handed mechanicking, and maybe a parking curb
incident on the back. Had to do some cleaning and gluing. Shoe
Goo, my favorite!
- The CD changer in the trunk had gotten flooded due to a clogged
drain in its side well. It was rusty, and is
unlikely ever to work again. One of the 3 wires to its
rusted electrical plug (there is also a 2-fiber optical plug) is
broken. I removed it, for now. We also vacuumed out the drain
holes.
- The open-box hitch was missing its mounting hardware. I dropped
about $15 at Ace for sufficient Grade 8 fasteners.
- The bumper cover was not clipped into one of the big guides on one
side.
- The bumper cover is composed of several parts clipped together,
and many of these clip connections were not seated correctly.
- We couldn't get the bolts to start on one side of the bumper cover.
Ended up having to take it all back apart and start over.
- We ended up short some plastic wedge clamps. Junkyard?
- One of the brake lights went out. Bad connection.
- Had to remove the 2" adapter from the bike rack.
- The first-aid kit that was stashed in the trunk wouldn't quite fit
into the rear armrest tray where it belonged. I re-packed it a
bit and now it fits in the tray.
The instructions from Curt call this an 80-minute job. We were at it
probably 5 hours, not counting our late lunch break while we let the
glue dry.
The trunk lid barely clears the rack, so it may be that we don't
really need its lowering swing-away feature. Time will tell.
Wednesday, August 25, 2021
Yesterday we bought oil change supplies at Wal-Mart. $42-odd for 2
5-quart jugs of 5W30 semi-synthetic and a Mobil 1 M1C-253A filter.
The oil was pretty black and glucky, it was long past time to change
it. I used the vacuum sucker, only a hair over 5 quarts came out.
(It had been complaining about low oil, but I didn't want to top it
off right before a change.) The old filter looked pretty deformed, it
was clearly long past its sell-by date. The O-rings on the plastic
filter stem were rock-hard, so I replaced them all (four) with the
ones that came with the filter. I put in 8 quarts of oil, and put the
other two in the trunk for top-offs. You don't have to pull off the
plastic engine cover to do this job, but it makes it easier if you do.
Tuesday, November 23, 2021
Snow tire day. Also added more oil, it has an appetite. (I bought
another jug of 5W-30 yesterday.)
Saturday, December 18, 2021
Car broke down on the freeway, on the trip to pick up Daniel from
college in Missoula. We were able to limp into Haugen, MT. The belt
tensioner idler pulley seized, and burned the belt off the car.
Without the alternator the engine only ran for a few minutes.
(Without the water pump, maybe it shouldn't have been run that long?
Temp gauge never climbed.) We were able to get safely off the
(snowing, and very hazardous) freeway under our own power, so that's
good. The dash lights were dimming and it started misfiring, barely
running at an idle speed, but it kept pushing us so that we could
actually take the freeway exit and park the car safely.
Tuesday, December 21, 2021
The recovery went flawlessly. We drove over in
the V10, dug out the car, put on the jumper
cables while we worked, and installed
the 'new' belt and pulley. (Chunks
of the old bearing fell out when I removed the old idler from the car.
The tensioner action felt very good, not stiff like the one on
Barney.) Checking all the belt-driven accessories by hand, the water
pump was very stiff, which is not a good sign. It's probably ready to
fail too. So, I used the old belt from Barney, rather than risk the
brand-new belt, just in case it did it again. (I had a tow rope
along, too, just in case.)
The engine started easily, but was a little squeaky. (Water pump?)
Regardless, we hopped in our vehicles and drove the 100 miles back
home, no incidents.
Wednesday, December 22, 2021
Checking the water pump at home, it's still stiff. Doesn't feel
'notchy' like a bad bearing, it's a straight grinding stiffness,
perhaps like the drive flange is contacting the face of the housing.
Regardless, it's defective and needs replacement.
It has been suggested that the suspiciously-short driving time after
the belt broke might be due to the battery being old and tired.
I checked my options, and decided to buy the NAPA water pump, which
could be picked up tomorrow. More money, but the car would be
drivable that much sooner. Total was $113.25, with tax and online
20% discount.
Thursday, December 23, 2021
Jill picked up the water pump. Daniel and I installed the water pump.
That was straightforward, but time-consuming. We put the car up on
ramps so we could drain the coolant out of the radiator petcock. The
drained coolant, just over 2 gallons, was green-black, I decided not
to reuse it. The spidery pump is held on with numerous E-Torx bolts,
in different sizes and lengths. A real PITA.
Once the pump was off the car the problem was obvious, especially when
comparing the two pumps. The shaft had worked inwards, allowing the
steel impeller to start milling a hole in the front of the aluminum
engine block. The pulley edge had also started cutting a groove in
the main hose neck. The old pump was not leaking, nor were its
bearings going bad. The geometry had simply slipped, you could see
that the drive flange was a bit out of plane, so it was the
shaft-to-bearing-race mating surfaces that had slipped out of
position, and not impeller-to-shaft or flange-to-shaft contacts.
The new Saleri pump, of course, did not have this problem. It came
with two gaskets, we used the formed O-ring style gasket rather than
the flat paper gasket. The only concern is that the milled divot in
the engine block might reduce the pumping efficiency, but there's next
to nothing that can be done about that, short of replacing the block
(!) or troweling JB-Weld into the divot and filing it flat. We'll try
it as-is first.
While the car was in the air I checked out the intermittent right-hand
fog light. The connector was burnt, but not the bulb's tab. New
bulb? I squeezed the connector to make a tighter connection and used
De-Ox-It on it. I also found that the connector on the exterior of
the housing was also going bad. I scraped/spread its connections as
best I could, and worked some stiff square-profile LED lead wire into
the sockets to tighten up the contact. And some De-Ox-It. With all
of that fooling around the connection seemed to be reliable again,
giving us both fog lights.
I also had Daniel work some bearing grease into the dry-sounding
idler, the one not on the tensioner. These are cheap and easy to
replace, unlike the tensioner idler. I'll do it at a later time, when
I figure out how to properly replace the bearings in the old idler.
We could only get half of the necessary replacement G-05 coolant back
into the engine. There was obviously an air bubble, and the heat did
not work. I got the engine heated up on a test drive, and parked it
nose up while it cooled. After a few hours this way, after dark and
with the snow starting, I moved it back into the garage. The car then
complained about low coolant, so the air bubble had been mostly
eliminated.
Friday, December 24, 2021
I added the rest of the coolant in two more burping steps today. Jill
drove the car to an evening gig, and all was well.
All that's left to do is to repair the original idler pulley, if I
can. I belive that it has to be repaired by drilling out the rivets
that hold the two halves together, and removing the bearing remains
from the insides. (Attempts to drive it out from either side
were abject failures.) Short screws (and plenty of thread locker!)
can be used to put it back together.
Monday, January 3, 2022
Yesterday I got the rivets out of the idler pulley, and the bearing
shell popped right out from the inside. (Grind off the thin side of
the rivets, carefully, and drive the bodies out with a
punch.) Today I bought a bearing, $14, and some #10-32 bolts, $4. I
think this'll work. Brown Bearing no longer takes cash,
and has a $25 minimum charge. I'll have to rethink using them in
future, I was not impressed.
The bearing is a Nachi 6203 2NSE9 C3, its specifications
are 17mm bore, 40mm OD, 12mm wide.
Monday, January 10, 2022
Daniel called from his job interview, the car wouldn't start
afterwards. I threw tools and jumper cables in the truck and went to
the rescue. The voltmeter showed only 12V on the resting battery, and
it dropped to about 11.6V when the door was opened. Bad sign!
Hitting the key to start showed it drop below 10V, which explained why
it didn't even try to run the starter motor. I used jumper cables to
give the car a bit of charge, and it then started. The running
voltage was around 14V, which is good. Bad battery? After charging a
bit I stopped the car and put the load tester on, and the battery
could only put out maybe 300A for a second or so before the voltage
dropped precipitously. There was no date code on the AC Delco
Group 49 battery, so who knows how old it is. It's at least 3
years old, as that's how long we've had the car. A weak battery would
certainly explain why the car ran for so little after
it threw the belt.
We made some calls, and eventually, after much screwing around, we
determined that Home Depot (in Liberty Lake) had an
H8/L5/Group 49 battery in stock, at $129, much less than other
potential sources. ($140.48 with tax.) We drove there directly and
bought one. I put the jumper cables on (to preserve system voltage)
and removed the old battery and installed the new one. This is fairly
easy to do, though it being under the rear seat is odd. A
post-replacement load test (after the nice drive to Home Depot) was
just as pathetic as before. I then returned the dead battery for the
$12 core.
Saturday, January 29, 2022
The new (cheap) idler wheel arrived today. $5.60 from FCP Euro.
Thursday, March 17, 2022
We dropped the car off at A&B Motors, to get the other front axle
replaced. (It had been 'grunching' badly for awhile, but we didn't
want to take one of our few practical 4wd vehicles out of service
during the snow season.)
Friday, March 18, 2022
$549.79 This is more than the $487.33 it was last
time.
Saturday, April 2, 2022
Found some Rain-X at the thrift shop for $2. IIRC this stuff works
great. Jill's going cross-State, so I put some on her car this
morning. We'll see...
Monday, August 1, 2022
Yesterday Jill complained of bad brake noises, and a wonky feeling in
the rear. I drove the car, and it definitely was metal-on-metal, not
just a rock caught in the brakes. I grounded the car.
Today Daniel and I jacked up the offending side of the car, and
examined the brake pads front and back. The front still had some
decent life left, but there was no material at all on the inner pad on
the back. Time for rear brakes! The inner surface of the rotor was
pretty badly scored, but I believe still usable.
We bought pads at NAPA, $50.95 for the four. (Sufficient for the rear
brakes.) We replaced the rears, the job was pretty textbook and we
were done in an hour. The big C clamp had no problem pushing the
caliper pucks back in, that's usually the sticking point on this job.
After the test drive all seemed normal again. Cleared to go, babe.
Saturday, October 1, 2022
Opened up the LR door, and removed the broken window regulator. The
usual plastic failures, had to drill out the four mounting rivets.
Wal-mart had the best price on a replacement regulator, believe it or
not: $28.10 shipped. I left the door panel off.
Wednesday, October 5, 2022
The rear dome light has been stuck on, and today I figured out why:
the light switch is not in the hinge area or inside the door, it's on
the body frame back by the latch. But with the door panel removed it
doesn't get pushed in enough to open the contacts. I cut a piece of
9mm shell casing as a cap to slip over the plunger, extending its
reach. That'll do the trick until repairs can be accomplished.
Also, one of the door panel retaining snap mounts had come unglued
from the door panel. A bit of Shoe Goo and it's back where it
belongs.
Monday, October 10, 2022
The new window regulator came a few days ago, and I finally had time
to install it. It took under an hour, and was remarkably
trouble-free. I used 5mm screws, washers, lockwashers, and nuts from
the shop stores in place of the drilled-out rivets. I used Spray 77
adhesive to reattach the moisture barrier. All fasteners are intact
and in place. I re-set the travel limits by holding down the switch
for the requisite five seconds.
Saturday, April 1, 2023
Low coolant again, in less than a week. This time I could see coolant
on the top of the oil pan flange. Water pump? But we just put on a
new one a little over a year ago. I topped
Jill off with water, put some in the trunk, and sent her on her way.
Friday, May 19, 2023
Recharged the AC, which has not been working. And, it's been hot.
(You can no longer buy R134a in Washington, so I went over to Wal-Mart
in Idaho a few days ago and bought two cans, at $10 each. Seems like
a rip-off to me.) The system still had some pressure so I put them
both in, and now the car's vent temperatures get down to about
53°F. Not great, but far better than nothing.
Monday, July 10, 2023
The 'temporary' tire I'd put on this Spring to take the place of the
one cracked 17" summer-tire wheel (which I can't seem to find a
reasonable replacement for) was starting to feel wobbly and bad, so I
swapped in another one from the pile. (Said 16" wheels being
intended for a second set of tires for Barney,
if/when.) The wobbling tire was having some belt material show
through, it looks like it could have been pothole or curb damage
coming to fruition. Jill's getting ready to go cross-State, and I was
uncomfortable with the tire situation. Good thing I checked.
Friday, August 4, 2023
She's been getting a brake pad warning, and today I had a cursory
look. Nothing overtly bad up front that I could see, though there's
only a single pad sensor (down from two on older cars) on each side.
There are no rear sensors. Fronts looked passable, rears looked
better.
Sunday, August 6, 2023
Today I had a better look look at the brakes. Yes, the LF sensor is
being cut into, so I'll order new front pads and sensors. The
replacement (and offsize) wheel/tire is actually the best looking one
now, the others are down to the wear bars. Probably time to replace
them next Spring. I might choose to steal the 16" wheels I
procured for Barney, rather than persist with the wretched 17"
wheels, one of which is cracked and useless.
I ordered pads and sensors from FCP Euro, $56.18 shipped.
Saturday, August 12, 2023
I installed the brake pads. This was straightforward, except that one
side's brake wear sensor had broken off inside its socket. Digging
that out took some time.
Of the four brake pads, three were still pretty usable, so they're on
the shelf for jalopy spares. Just in case.
Sunday, August 13, 2023
I stopped at the junkyard and found two more 16" wheels. I think
the 17" tires are nearing EOL, and I now have no intention of
purchasing more in that size. (I need two more wheels in order to
make all six of our potential active sets be 16", leaving three
17" wheels potentially up for sale.)
I also picked up a vent assembly, though it is the wrong color.
Perhaps I can move the knob over to the car?
Friday, August 25, 2023
I tore into the vent assembly, you can get the louvers out by pulling
the little metal hinge pin out of the outboard side of the vent
louvers. However, I don't see how the knob can be removed from the
louver itself.
Sunday, September 3, 2023
Jill reports that the D2R low-beam headlamp on the driver's side is
out. I thought I'd noticed a color change recently, which is a sign
of impending failure on these. I ordered a pair of D2R 4,300K bulbs
from DMEX via Amazon, $32.42 shipped.
Wednesday, September 6, 2023
Jill reported that the high beam on the driver's side also appeared to
be out. I investigated, and while it's not exactly out it's quite dim
in comparison to the passenger-side light, yet the color temperature
matches. WTF? I'll investigate further once the replacement D2R bulb
comes.
Friday, September 8, 2023
The D2R bulbs came yesterday. I installed one today. Such a
difference when compared to
the hour-long cluster-fuck that is
that job on the X5! Simply release the bayonet locks on the hatch
cover, socket, and the bulb retaining ring, replace the bulb, and
reverse to reassemble. Done in under a minute, if you've done it
before.
As planned, while I was there I investigated the puny high beam on
that side. Apparently the bozo who last replaced the H7 bulb didn't
get it bayonet-locked into place, so it had fallen back into the
housing away from the focus point of the reflector. I re-seated it,
properly I hope, and it's now a lot brighter. To gain access to the
high-beam hatch you have to slide the headlight-washer reservoir up
and out of the way.
Also, some ham-handed SOB broke the bayonet lock on the city (parking)
light socket in the same housing. (Push and twist, gently, to remove.
Don't force it!) While I have another bulb holder from a spare
non-HID headlight I bought I'd have to cut and solder the socket in,
and that'd leave the donor headlight assembly, which has nice clear
lenses, crippled. Not really worth it, I just wrapped electrical tape
around the socket body so it fits more snugly without the bayonet
lock, and pushed it into place. I think it'll be good enough.
Saturday, September 9, 2023
For grins I ordered a pair of H7 6500K (the only color temperature I
can find in this form factor) LED replacements from Suparee/Amazon,
$43.23, to see if they will be brighter than the high-beam halogens.
High beams are much less critical about light pattern details than
lows, and so long as the deer-spotting ability is good I'm OK with
that. And LEDs are likely to fit better than the lame-ass D2S HID
bulb kits I could find, and are instant-on so the 'optical horn'
function should be good. I have concerns about their potential
longevity, but these look like they've better heat sinks than some
that are in this same form factor as the halogens, so they ought to
fit, physically anyways. (And the heat will be inside the
lamp shell, and so should help keep the lens clear under snow/ice
conditions, unless the bulbs cook to death.) The only real concerns I
have at the moment are the lamp-out detection system, and longevity. I
guess we'll see.
Sunday, September 10, 2023
It is suggested that the 210 826 05 82 clearance light
socket assembly could replace the broken city light socket. I ordered
one.
Thursday, September 14, 2023
The H7-equivalent LED lamps came today. I installed them. First I
put an H7 in the spare junkbox headlamp to see what stock lighting
looked like, aimed around the yard at night. Surprisingly feeble,
with a rather short-height high-beam bar of light. But it works well
on the road. (I drove the car with the properly-installed H7 in it,
the high beams are indeed much better this way. So, that had
been a problem ever since we got the car.) Then I put in an LED lamp.
Nothing exploded, and light came out. The pattern looked pretty
similar, but did seem perhaps 2× as bright, and was certainly
whiter. (Verging on blue-ish, but I don't think objectionably so.
And, these are high beams, so how they appear to oncoming drivers is
largely irrelevant, since they shouldn't be on in those conditions.)
Testing, such as it was, passed, I installed the new lamps in the car.
That was a bit fiddly, it looks like the bulbs are intended to go in
multiple ways, just in case they have to be rotated due to the
unavoidable directionality of the LEDs vs the reflectors. (Probably
for use with low beams, which I would not do. I also noticed that the
city light socket on the other side is also broken, and was wedged
into place with a wad of blue paper towel. Perhaps I should have
ordered two replacements?) I then took another test drive.
Yes, noticeably brighter. The light pattern seemed good while
driving, and turning high beams off made the lighting seem much
dimmer, which was not the case when I first started investigating.
We'll see how these hold up, I put the old H7s in the trunk just in
case the LEDs crap out on the road. There were no lamp-out
indications, which is good. (Some cars don't like some LED bulbs.)
Also, both fog lights are now out. Again. Will definitely need to
look into those next, though true need for them is rare.
Sunday, October 1, 2023
Yesterday the new low beam was out. Grr! I investigated, and found
that the lamp had merely come unplugged. (The new high beams have
been working well.) I plugged it back in. It does have a bayonet
lock, but it doesn't take much of a twist to release it, and the
moment arm of the cable could be a contributor. (A pothole might have
done the job.) While I was there I removed the very bad city light
socket, and checked that the new one fits. Yes, it does. I cut off
the ends of everything and spliced the new socket in, using solder and
heat shrink tape. I moved the bulb over and put it back together. It
all works.
On a roll I had a look at the again-defunct fog lights. The
connectors again weren't making good contact. I was able to peel the
shells off of the female connections in the wiring harness, and get
down to the metal connectors themselves. I scraped them out, then
used a piece of 14ga solid copper wire to prevent collapse, and used
pliers to close up the spring connections. After reassembly, scraping
the male pins and treating with De-Ox-It the driver's side worked
properly. (These connectors are very badly designed, except for the
fact that the shells can be opened.) The fog lamp assembly was
missing a 8mm hex screw holding the unit in, so I replaced it from the
junk box.
On the passenger side, one of the two male pins in that lousy
connector had corroded away to nothing. I was able to twist the
carcass out with needlenose pliers. The pin is roughly the size of
12ga solid wire, so I cut a length of same and shaped it to be like
the pin. I soldered it to the high-temperature wire end. It fits
snugly into the plastic shell, but lacks any kind of locking mechanism
like the original pin had. After reassembly this light also worked
again.
I think I'll want to put in extra-bright H1 yellow LED equivalents, if
I can find some. These fog lights are ultra-feeble, and could use some
more lumens.
The LR door wouldn't shut last night either. Today I took off the
panel. What I found is that the door release cable has perhaps
stretched a bit, and was now slightly pulling on the latch, preventing
it from catching unless you pushed in on the interior release as you
shut the door. However, when the panel came off one of the glued-on
bits of the door panel popped off, so I used Shoe Goo to reattach it.
However, that puts glue-drying time into the project. Sigh.
Tuesday, October 3, 2023
Another fastener on the door panel came loose yesterday, so I had more
gluing to do. This morning I put the panel on, the door seems to work
correctly. I think the real problem was lubrication, a spray of WD-40
into the latch seems to have helped.
I believe the RF wheel is out of round, or out of balance, so I popped
it off. I didn't see anything, but the tread is very low. I'm
thinking of having the tire from the bad wheel swapped onto it. I
looked at the oddball LF tire too, and it seems fine. Since I had the
front wheels off I installed brake bleeder caps from the junk box.
I stopped by Schwab this morning and had the tires swapped. I think
it helped, but not a lot.
Road trip!
Tuesday, October 10, 2023
The RH city light is out. 64132, or H6W, or BAX9S.
Saturday, November 11, 2023
I had ordered some yellow H1 LED bulbs and some BAX9S LED replacement
bulbs recently, and today I installed them in the car. Everything's
nice and bright, and I'm not seeing any lamp-out shenanigans. So far
all the LED replacements have been very good, I should look into
beefing up the backup lights, and the rear fog light.
Sunday, March 24, 2024
One of the BAX9S LED replacement bulbs failed recently, and I bought
another replacement. (The bulbs were entirely satisfactory, while
working.) I also ordered two types of 1156 backup light replacements,
and a red one for the rear fog light. I installed them all in the car
today. The less-directional (but somewhat brighter) white lamp is
marginally better than the incandescent, the red doesn't really look
any different than the incandescent. I was really hoping for
substantially more lumens in these applications, oh well.
Friday, March 29, 2024
Swapped on the new set of $750 summer tires, it's well past time.
I'm getting lamp-out indications at power-on, which is odd.
Thursday, May 23, 2024
The LR door wouldn't close again. I pulled the panel and messed with
the latch, and eventually got it closing again. But there were glue
failures, so can't put the door back together yet.
Saturday, May 25, 2024
I started to repair the door panel, with glue.
Saturday, June 1, 2024
Yesterday I put back the door panel, and removed the broken sunvisor.
I glued its plastic hinge socket back together with Shoe Goo, and used
a ring of brass from a shotgun shell as a collar to strengthen it.
Dried, today I reinstalled it. I think it'll be fine.
Friday, July 5, 2024
Added some more coolant, it was complaining.
Wednesday, July 10, 2024
Coolant low again, signs of leaking off the front of the engine.
Dropped car off at A&B.
Friday, July 12, 2024
Picked up car. $892.12 for new water pump and thermostat. Invoice
31895.
Friday, October 4, 2024
The other new LED parking light (BAX9S) has also failed. I replaced
it with the last spare. Cheap Chinese shit.
Monday, December 16, 2024
The car's been misfiring, and running on reduced cylinders
occasionally for awhile. (A restart necessary to get back to normal.)
We took it in, and got (12) new plugs and new spark plug wires, which
all apparently looked very bad. (Missfires on 1, 4, 5, & 6, plus
random. [Codes P030[01456].] Parts cost $620, expensive! Hoping it
isn't coil packs too, we'll try just this first.) $1,361.25 at
A&B. Invoice 31969.
Tuesday, December 17, 2024
Picked up a bolt in the RF snow tire. Wasn't detected until we got
down the hill onto the pavement. Ruined? Schwab wouldn't fix it,
tire too worn?
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